429CV23
Member
Hey all
I finally got around to rebuilding the S&S Shorty G on my 2000 Bulldog with S&S 107"; Bassani 2-into-1.
It ran fine before, but leaked fuel if I left the petcock open, and was running lean on the intermediate jet; discolored headers, some popping on decel I couldn't tune out.
I increased the intermediate from 0.031" to 0.032"; I left the 'original' main jet in, an 0.082". I never had an issue with the 3000+ RPM range before the rebuild. Now it runs strong for 5-10sec, then starts cutting out. I did not adjust the float. According to the tuning guide, this condition would require an 0.004" increase, but it seems an 0.082" is fairly large to begin with.
The PO did install a spike (forward facing) which I was going to remove, but am missing some hardware to install the original filter setup, which has a K&N filter with it. The brace for the spike was broken on the forward side, so I welded it to regain support for that heavy spike.
I know the engine was rebuilt once by the original owner, and I was told it pulled 120tq on a dyno (no reported hp #), but an 82 main still seems large.
I think if the broken brace was causing an air leak, it would be running richer now, so why the higher RPM breakup?
I finally got around to rebuilding the S&S Shorty G on my 2000 Bulldog with S&S 107"; Bassani 2-into-1.
It ran fine before, but leaked fuel if I left the petcock open, and was running lean on the intermediate jet; discolored headers, some popping on decel I couldn't tune out.
I increased the intermediate from 0.031" to 0.032"; I left the 'original' main jet in, an 0.082". I never had an issue with the 3000+ RPM range before the rebuild. Now it runs strong for 5-10sec, then starts cutting out. I did not adjust the float. According to the tuning guide, this condition would require an 0.004" increase, but it seems an 0.082" is fairly large to begin with.
The PO did install a spike (forward facing) which I was going to remove, but am missing some hardware to install the original filter setup, which has a K&N filter with it. The brace for the spike was broken on the forward side, so I welded it to regain support for that heavy spike.
I know the engine was rebuilt once by the original owner, and I was told it pulled 120tq on a dyno (no reported hp #), but an 82 main still seems large.
I think if the broken brace was causing an air leak, it would be running richer now, so why the higher RPM breakup?